Okay, Im experiancing a loss of power just after each shift, the only way the keep it from loosing power is to keep the rpm’s up above 3 g’s meaning i have to tacked out before shifting.
Also so when i press the clutch in she drops down to almost 4-500rpm?
Im running new NGK plugs already
Replaced the distributor cap and rotor
replaced plug wires
running a short ram intake
Any suggestions?? Thanks
Thanks for the suggestions guys, I just knew when I titled it “serious” that ya’ll would come and help. Im going to get some more “vtec” fluid right now, I origanally thought it was only for Hondas, but I can try it they said, and the crack juioce??? I guess you mean Lucas, so im going to add some more now… :kekegay:
I have not, That is a good idea thank you, I dont know if this would have anything to do with it, but the MAS has been replaced a few times, and i know that sometimes it idles rough, butu if i hold it around 2500 for a min, it then runs fine??? but im checking the vacuum llines here in a min.
Bump, any more suggestions, i havent found a vac leak yet, i put 93octane in iut today but dont see a differance, and i pulled the plugs and found then pretty black even thoough they have only 500 miles on them?
No potatoe in the tail pipe. Ive had that problem before, still cant figure out how they grow in thier :dunno:
No clog in the cat.
Actullly about 2 weeks ago the pipe had a whole in it so i removed the cat awaiting a new exhaust.
and now the pipe entering the muffler is broken from beating the pipe expander on.
Do you think lack of back pressure is causing this?
Well if motor is screwed up, thats good cause that will force the sr20det, but i’d like to run this engine another year, so without a a/f gauge how do i measure it, and if like a previous post mentioned the distributor is screwed up, can i buy one rebuilt or new or??? I ve never changed that before.
-Thanks guys for the suggestions
then its prob ignition, or somethen else dumb like and air filter or somethen, i had a similar problem when my hatch still had 73hp, it endded up a wire in the dizzy being loose…