Geez! Not sure why, but it looks like the middle layer failed, and blew through a good part of the head gasket. I hope this is the only cause of my severe coolant pressurizing!!
Any ideas of what would have caused this? My theories are detonation on that cylinder, possibly the head not being torqued down enough, or a faulty gasket.
You’re supposed to be the Neon guy! :mamoru: But I would have to assume it didn’t seal too well considering they fixed the HG issues in 98. I thought about removing the HG shim (middle layer) last week for a couple ponies, good thing I reconsidered.
It was pressurizing the coolant system so bad, I couldn’t keep any coolant in it! I am pretty sure it was from running lean, and it blew out the gasket, maybe a combination of that and not being torqued down enough.
I didn’t install megasquirt on it for the previous owner until late last year, so up until then, it was probably running wicked lean.
At least the block is cast iron, so its more resiliant, but its still worth checking! I will probably have the machine shop here check the head over, deck it if neccessary, and then check the block over good with a straight edge to check for any problems!
Yeah, cylinder 1 does run the leanest, now that I think about it. It could have been all very lean, and this is the first one to go since it was on the end, or it could have been a bad injector, any number of things. I will get it looked it, I just hope that head is ok! One side of the head gasket was mint, and the other was crappy, so hopefully it didn’t do too much damage. Even if it did, nothing I haven’t already done on these stupid fucking cars, hah.
Some good news is that this combustion chamber on the far right is the one that had the bad head gasket, and it doesn’t have visible black marks to the right of the chamber, so that is the first good sign:
Plus the failure for stock Neons was not anything like this failure. It resulted in an oil leak on the exhaust side of the #4 cylinder. Not a lean blow-out on #1.
Correct. I bought it with a bad motor, knowing that I would be fixing it up. I had hoped from day 1 it was a head gasket issue, and not a cracked block or head, and this gives me more hope that my initial diagnosis was correct!
Can’t say for sure yet, but it looks that way. There are no obvious “burn” marks on the head. I will have it looked over, but I think we dodged the bullet here!