OK. update.
We’ve tried to bleed it 2 more times.
We’ve replaced The bottom hose, replaced the hose clamps
also, re-done the water pump seal…
after doing this, it felt like success for these reasons. When bleeding, we threaded the bleeder screw in just a couple notches, so that air could come out but coolant couldnt, it would kind of bubble or fizz around the edges.
by the time the motor got to operating temperature (which happened fairly quickly, mucher faster than usual) we turned the heat on full blast, and ACTUALLY FELT HEAT! this is the first time ive felt heat from the blowers in months.
Bleed it some more, revving off and on, en take it for a test boot. still blasting heat from the blower, im pretty much free revving along as it was last night, the snow was falling nicely, i may or may not have gotten sideways hither and thither…
but now the temp gauge starts creeping ever so slowly… 2.5 notches from H.
so i figure ok air bubbles perhaps…
head to try bleeding more, heat no longer blowing inside
bleed it more, now i have the boiling coolant problem again
oh and it seemed to have taken a TONNE more coolant the second bleeding attempt.
but… this morning the rad wasnt really low.
i cleaned up the motor a bit, now im checking periodically to see if coolant is developing…
So basically… things were looking REALLY good… perfect almost…
then it quickly went to shit again.
but… i am getting closer. Ive been observing the temperature… and now i dont go full H very often… and, the temperature is very inconsistant, ill be getting hot, then cool down again, then get hot. I thought it may have to do with RPM, but i booted 5th gear to 3K and the temp went down.
This lead me to beleive that it was just because i was going fast = more air flow for rad… but then it got hot again. Then i drove at 3K in 3rd, cooled down. driving regularly in a gas saving type way, the temperature is inconsistant then as well.
But still not FULL H all the time, which is what was happening last week. no matter how i drove the Temperature only rose without getting the RPMs low, or just turning it off.
theories… Water pump seal might have been solid for the test boot, but due to cold and the gasket not setting correctly… ruptured and let air back into the system. perhaps now the seal is better than before, but still not right.
and, then theres the idea that maybe im still not bleeding it correctly.
sigh.
i want my baby back